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| 15) Finally, the end tanks were fabricated and welded onto the cores with the four #8 water hose bunges and fill cap. In this view I'm lapping the mating surface after post weld machining using a flat table. |
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| 16) After quite a bit of analysis I decided the stock intake manifold left quite a bit to be desired and put a major restraint on my design goals. The stock manifold is a fine piece of engineering, combining the flow and accustic properties of both a single plane and dual plane manifold into one with it's variable volume system. However, it had two drawbacks in my mind. One, it required the air flow negotiate a significant turn (for packaging considerations I suspect). Two, the casting has very thin walls to keep weight down and therefore the intake opening could not be increased to my design spec of 3". Therefore, to incorporate a larger more direct entry for my 3" dia IC to main intake manifold tube size it had to be heavily modified. This mod began with the "beheading" of the stock intake snorkel from it's upper casing as shown above. |
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| 17) With the TB portion of the intake essintially chopped off, I needed to create an interface for a new intake entry manifold into the main plenum. I sized an opening and machined an interface plate for this purpose. The problem is that the stock manifold is multi-piece and split at my new interface. Therefore, I needed to split my interface plate and weld one each to both top and bottom castings. The top casing and welded on interface plate is shown above. Also note that the EGR distribution network has been machined away revealing the actual individual EGR ports in each intake runner. These were welding closed. |
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| 18) Here's a view of the same upper casing from the bottom. The center divider is removed and the edges radiused. After welding, the engine mating surfaces were fly-cut flat. |
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| 19) The stock variable volume butterfly housing became the building block for my lower manifold housing. The butterflys were removed and all associated material machined away. The upper and lower housings were bolted together and the lower section of my split interface flange was located and tacked in place. In addition, individual pieces of 6061 T6 were cut to size were tacked in place to complete the "belly pan" part of the main plenum. Plenum size was selected to complement mid to high speed performance. Final welding and machining was done on individual parts and as an assembly to square things up and ensure good sealing at all interfaces. |
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| 20) To create an optimum transition from IC feed tubing to main manifold yet another fabricated housing is required. This one is made using 3/8" 6061 T6 for the bolting flange and two hand shaped sections of 3" dia 0.075 wall 6061 tube for the main body. Two bunges were added, one for the power brake vacuum take-off and the other for the IAT sensor. Additional vacuum ports can be seen on the lower righthand side. These are used for the fuel pressure regulator, MAP sensor, bypass valve and dash mounted boost gage. The housing was clamped in position on the main manifold and all holes piloted and matchdrilled. Holes in the main manifold flange were then opened and tapped for the 8 attach bolts. |
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| 21) The entire Main manifold assembly (upper manifold, Belly pan and transition manifold) were pressure tested to look for leaks. Note the bar plates covering the runner openings. The only surprise found during this test was that those fancy $10 each "T" bolt hose clamps are worth a SH--! At least when were talking medium boost levels. No matter how tight I torqued them, lubed the hose (silicon grease), or rotated them they still leaked at all the clamped interfaces (particularly if the interface wasn't PERFECTLY round). I suspect it has something to do with the rather low local clamping pressure on these wide band type clamps. I replaced them with good quality stainless steel worm type clamps (as shown) and the problem immediately disappeared. Now I'm not saying you'll loose much boost as the leak rates would be relatively small compared to the total flow, but it was still very interesting. That's about 12 psi on the gauge. |
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| 22) A view showing both manifolds bolted to the engine. Note: Optimum air-flow entry has some side affects. In this case, interference with the thermostat housing assembly (removed in this shot). Several modifications to the thermostat housing needed to be performed to remove the interference. In addition, the IAC (idle air controller) and fast idle valves were discarded. The IAC is not a big deal for my purposes as I can adjust my idle speed the old fashion way, at the throttle body. Adding a few hundred rpm to the basic idle speed adequately compensates for additional engine loads and varying environmental conditions. The loss of the hot idle circuit simply means I need to keep engine speed up using my right foot while warming the engine . |
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| 23) One of the major changes to the thermostat housing is the complete removal (cut off) of this particular part of the casing and subsequent sealing of same. It houses water circuits for the hot start valve (small tap), coolant tank feed ( med tap), and passenger compartment heater return (large tap). All but the hot start tap were re-established at other non-interfering locations. A better perspective of this mod can be seen in the "Thermal Control" section |
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| 24) Before the Supercharger assembly could be mounted some additional modifications to several support systems needed to be done. For example, the location of the pressure side fuel line to the fuel rail need to be moved due to interference with the S/Cer support plate. I machined off the stock fuel rail to line interface boss and welded it closed. I then machined the forward end of the rail to accept a #8 AN bunge and welded it in place. A new fuel line from the stock filter was fabricated, routed and installed as shown. 550cc RC injectors were also installed. Note the fuel pressure sensors incorporated into the banjo bolt on the rear bank fuel rail. Detail on this mod can be seen in the engine management section. Also shown is a lengthened alternator lead, re-routed harnesses and the front S/C support which also secures the belt tensioner pulley and Idler pulley. Note, the belt routing shown in this picture was the revision A design, not the initial design. Another key item is the elimination of the PCV valve and incorporation of a second valve cover vent on the front bank. Both vent and PCV hole are attached to a the same breather hose and routed to the catch can. Oil in the air stream in any form via the PVC valve, bad valve seals, blow-by hose or poor oil control rings leads to detonation and must be avoided. Hence the removal of the PVC and blow-by recirculation systems. |
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| 25) Here's the S/Cer blower assembly ready to bolt on the engine. Once the S/Cer assembly is mounted the IC can be bolted in place. I machined a small adapter so that the stock throttle positioner could be used on the Accufab Ford throttle body. Support strut is made of graphite. The funny looking tube jogging out from the TB manifold is the bypass tube. |
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| 26) This shot shows quite a few things. Significant are: The re-location of the coolant tank air separator spigot on the thermostat housing (see directly under new manifold on lefthand side), addition of the ICs upper and lower water tanks along with it's pressure and return water lines (note; flow is bottom to top), tacked together IC to main intake feed tubing. |
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| 27) Another view of the overall air flow system. Take note that the air flow from throttle body to intake runners is as short as possible with large radius bends (as few as possible) and smooth transitions. Note the dual IC water hoses. Due to the need to keep the overall IC profile as low as possible to allow adequate dynamic clearance to the hatch glass, the end tanks needed to be half height. This dictated that two #8 size fittings be used as opposed to one #12. |
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| MSC Performance NSX S/C |